Well I got it all set up, took longer than I thought, but it fired off right away once fuel made it to injectors. I heat cycled it, sorta, like some of the big performance people for HD advise, not sure its necessary on a stock engine. It acts normal so I'll have to ride it later on in the week. Sure sounds good, we'll see how it goes. I still have to post pics on the various mods I did. Some could be viewed as good or bad, we'll find out.
Changes: Hi lead bronze for mains (#936) with left side not grooved and made with integral thrust face (orig thrust washer must have gotten tight and ripped anti rotation tabs off). Right side main grooved. Both set at 0.005" interference fit at room temp, bored to size with 0.0015" oil clearance. Had piston skirts recoated by Swain and crown ceramic coated (it's not much more when you do both) had chambers and exhaust ports ceramic coated as well as valve faces. Running total seal gapless top ring set (Ive never ran a set so I thought I'd try one) replacement teflon scavenging pump bushing had failed, tried aluminum which came in spare engine I never used. Finish honed opening up 0.0005" with 180 grit Sunned AN followed by Sunnen plateau hone inserts. Factory head & base gaskets with stock head bolts.
Its amazing this engine ran the way it did with as much that was wrong with it. I came away with a different opinion in the design as it appears to be well made other than the mains which may come loose due to loss of fit. I was really impressed how straight and round the cylinders were. Hardly any scoring evident, which for a demonstrator bike is impressive. Although this bike was only #14 on build list it has the later crank and compensator drive, so question begs was the factory engg. team evaluating the new parts?? In 14k miles the exhaust valves were not looking new anymore, had Atlantic EH tune dropped in shortly after I got it at about 7200 miles. I didn't realize it at the time but right side main had already spun at that point so I rode this machine 7800 miles with bearing out spinning in case...... who knows when it started....talk about lucky...... if it were the right side the rods would have smoked as both are fed from right side. It didn't hurt crank at all, main opened up case bore a few thousandths. Truly amazing it didn't shell out one way or another.